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Dennis Donovan

Dennis Donovan's Journal
Dennis Donovan's Journal
February 21, 2019

Syracuse basketball coach Jim Boeheim hits, kills man walking on interstate

Source: CNN

(CNN)Jim Boeheim, longtime head coach of the Syracuse University men's basketball team, hit and killed a pedestrian who was walking along Interstate 690 late Wednesday in upstate New York, according to a police statement obtained by CNN affiliate WSYR.

In the statement, Syracuse police said a 51-year-old man was on the side of the highway after a vehicle he was in lost control and struck a guardrail.
Boeheim, 74, was driving and noticed the vehicle, which was in the middle of the roadway. Boeheim moved to avoid the vehicle and ended up hitting the man, police said.
Police said they were called to the initial accident at about 11:22 p.m.
The man who was struck was taken to a hospital, where he was pronounced dead, according to Syracuse police.

Read more: https://www.cnn.com/2019/02/21/us/jim-boeheim-syracuse-kills-pedestrian/index.html



February 21, 2019

Martha Quinn...

...discuss.

February 21, 2019

"Take On Me" Video... by Weezer?





1985!
February 20, 2019

Jill Wine-Banks' pin today:

https://twitter.com/JillWineBanks/status/1098248272282566657


#JillsPin is a sign of the Trump era, keeping prosecutors and investigators busy. Join me on #MSNBC on @mitchellreports at 11 am CT/noon ET for analysis of latest news about DOJ, Mueller, Whitaker, Barr, McCabe, SDNY and more.


February 20, 2019

48 Years Ago Today; EBS False Alarm of 1971



https://en.wikipedia.org/wiki/Emergency_Broadcast_System#False_alarm_of_1971

False alarm of 1971
A properly authenticated Emergency Action Notification was incorrectly sent to United States broadcast stations at 9:33 a.m. Eastern Standard Time on February 20, 1971. At the usual time a weekly EAN test is performed, NORAD teletype operator W. S. Eberhardt had three tapes in front of him: a test tape, and two tapes indicating a real emergency, instructing the use of EAN Message #1, and #2, respectively. He inadvertently used the wrong tape, with codeword "HATEFULNESS". This message ordered stations to cease regular programming immediately, and begin an Emergency Action Notification using Message #1. Message 1 states that regular programming has been interrupted at the request of the United States government, but is not specific about the cause. A cancellation message was sent at 9:59 a.m. EST, but it used an incorrect codeword. A cancellation message with the correct codeword, "IMPISH", was not sent until 10:13 a.m. EST After 40 minutes and six incorrect or improperly formatted cancellation messages, the accidental activation was officially terminated.

This false alarm demonstrated major flaws in the practical implementation of an EAN. Over 2,500 radio and television stations received the notification. Some stations ignored it (convinced it was false because it came at the time of a scheduled test) and continued with regular programming. Others cancelled the EAN prematurely, with or without an any coded indication that the alert was erroneous. Still other stations did not have EAN procedure documents readily accessible to them, so they had no indication of what to do at all. It is estimated that only 20% of the stations that received the activation followed the procedures completely. Several stations went off the air, as they were instructed to do. Recordings from stations that did not (and were not supposed to according to EAN procedures) include one from WOWO in Fort Wayne, Indiana, for which a recording of the EAN activation exists. Another recording of the EAN activation on WCCO in Minneapolis/Saint Paul, Minnesota can be heard on RadioTapes.com.

This false alarm was sufficiently disruptive to move the FCC to temporarily suspend use and testing of Emergency Action Notifications (EANs) by codeword effective February 25, 1971. In the meantime, a national EBS activation (actual or test) would be routed through news service broadcast desks, then authenticated with the White House communications center, introducing a delay of approximately one minute.[9] Numerous investigations were launched, and several changes were made to the EBS. Among them, EAN Message #2, which contains specific language indicating an imminent attack, was eliminated. Another change was moving the tapes for genuine alerts away from the broadcasting machines to prevent them being mistaken for the weekly test tapes. After numerous safeguards were put in place, the FCC voted to resume automatic national activation of the EBS using EANs in mid-December, 1972, almost 20 months after they were suspended.


I was 5 at the time and in Kindergarten. I don't recall this happening, though.
February 20, 2019

16 Tears Ago Today; The Station Nightclub Fire kills 100

https://en.wikipedia.org/wiki/The_Station_nightclub_fire



The Station nightclub fire

The Station nightclub fire occurred on Thursday, February 20, 2003, in West Warwick, Rhode Island, killing 100 people and injuring 230. The fire was caused by pyrotechnics set off by the tour manager of the evening's headlining band Great White, which ignited plastic foam used as sound insulation in the walls and ceilings surrounding the stage. The blaze reached flashover within one minute, causing all combustible materials to burn. Intense black smoke engulfed the club in 5½ minutes. Video footage of the fire shows its ignition, rapid growth, the billowing smoke that quickly made escape impossible, and blocked egress that further hindered evacuation. The toxic smoke, heat, and the resulting human crush toward the main exit killed 100; 230 were injured and another 132 escaped uninjured. Many of the survivors developed posttraumatic stress disorder as a result of psychological trauma.

It was the fourth-deadliest nightclub fire in US history, and the second deadliest in New England, surpassed by the 1942 Cocoanut Grove fire which resulted in 492 deaths.

Fire
The fire started just seconds into the band's opening song, their 1991 Billboard Mainstream Rock hit "Desert Moon", when pyrotechnics set off by tour manager Daniel Biechele ignited flammable acoustic foam on both sides and the top centre of the drummer's alcove at the back of the stage. The pyrotechnics were gerbs, cylindrical devices that produce a controlled spray of sparks. Biechele used three gerbs set to spray sparks 15 feet (4.6 m) for 15 seconds. Two gerbs were at 45-degree angles, with the middle one pointing straight up. The flanking gerbs became the principal cause of the fire. The acoustic foam was installed in two layers, with highly flammable urethane foam above polyethylene foam, the latter being difficult to ignite but releasing much more heat once ignited by the less dense urethane. Burning polyurethane foam instantly develops opaque, dark smoke along with deadly carbon monoxide and hydrogen cyanide gas. Inhaling this smoke only 2-3 times would cause rapid loss of consciousness and, eventually, death by internal suffocation.

The flames were initially thought to be part of the act (the song's music video clearly shows flames blazing around the musicians); only as the fire reached the ceiling and smoke began to bank down did people realize it was uncontrolled. Twenty seconds after the pyrotechnics ended, the band stopped playing and lead vocalist Jack Russell calmly remarked into the microphone, "Wow... that's not good." In less than a minute, the entire stage was engulfed in flames, with most of the band members and entourage fleeing for the west exit by the stage.


Number of victims found by location (main exit at bottom-center)

By this time, the nightclub's fire alarm had activated, and although there were four possible exits, most people headed for the front door through which they had entered. The ensuing stampede led to a crush in the narrow hallway leading to that exit, quickly blocking the exit completely and resulting in numerous deaths and injuries among the patrons and staff. A total of 462 people were in attendance, even though the club's official licensed capacity was 404. One hundred lost their lives, and about half of the survivors were injured, either from burns, smoke inhalation, thermal trauma, or trampling. Among those who died in the fire were Great White's lead guitarist, Ty Longley, and the show's emcee, WHJY DJ Mike "The Doctor" Gonsalves. There is reason to believe that Longley and Gonsalves tried to salvage equipment during the early stage of the fire and lost valuable time to escape before dense, toxic smoke made breathing near impossible at zero visibility. Longley is believed to have initially made it out of the building but then re-entered in an attempt to rescue his guitar. Furthermore, a number of survivors later stated that a bouncer stopped people trying to escape via the stage exit, stating that that door was "for the band only."

The fire, from its inception, was caught on videotape by cameraman Brian Butler for WPRI-TV of Providence, and the beginning of that tape was released to national news stations. Butler was there for a planned piece on nightclub safety being reported by Jeffrey A. Derderian, a WPRI news reporter who was also a part-owner of The Station. WPRI-TV would later be cited for conflict of interest in having a reporter do a report concerning his own property. The report had been inspired by the E2 nightclub stampede in Chicago that had claimed 21 lives only three days earlier. At the scene of the fire, Butler gave this account of the tragedy:

...It was that fast. As soon as the pyrotechnics stopped, the flame had started on the egg-crate backing behind the stage, and it just went up the ceiling. And people stood and watched it, and some people backed off. When I turned around, some people were already trying to leave, and others were just sitting there going, 'Yeah, that's great!' And I remember that statement, because I was, like, this is not great. This is the time to leave.

At first, there was no panic. Everybody just kind of turned. Most people still just stood there. In the other rooms, the smoke hadn't gotten to them, the flame wasn't that bad, they didn't think anything of it. Well, I guess once we all started to turn toward the door, and we got bottle-necked into the front door, people just kept pushing, and eventually everyone popped out of the door, including myself.

That's when I turned back. I went around back. There was no one coming out the back door anymore. I kicked out a side window to try to get people out of there. One guy did crawl out. I went back around the front again, and that's when you saw people stacked on top of each other, trying to get out of the front door. And by then, the black smoke was pouring out over their heads.

I noticed when the pyro stopped, the flame had kept going on both sides. And then on one side, I noticed it come over the top, and that's when I said, 'I have to leave.' And I turned around, I said, 'Get out, get out, get to the door, get to the door!' And people just stood there.

There was a table in the way at the door, and I pulled that out just to get it out of the way so people could get out easier. And I never expected it to take off as fast as it did. It just—it was so fast. It had to be two minutes tops before the whole place was black smoke.


Aftermath
Thousands of mourners attended a memorial service at St. Gregory the Great Church in Warwick on February 24, 2003, to remember those lost in the fire. Following the tragedy, Governor Donald Carcieri declared a moratorium on pyrotechnic displays at venues that hold fewer than 300 people.


Makeshift memorial at the site of the Station night club

Five months after the fire, Great White started a benefit tour, saying a prayer at the beginning of each concert for the friends and families affected by the incident and giving a portion of the proceeds to the Station Family Fund. In 2003, and again in 2005, the band stated they had not performed the song "Desert Moon" since the tragedy. "I don't think I could ever sing that song again," said lead vocalist and founder Jack Russell, while guitarist Mark Kendall stated "We haven't played that song. Things that bring back memories of that night we try to stay away from. And that song reminds us of that night. We haven't played it since then and probably never will." By 2009, however, the band had resumed performing the song.

Two years to the day after the fire, band members Jack Russell and Mark Kendall, along with Great White's attorney, Ed McPherson, appeared on Larry King Live with three survivors of the fire and the father of Ty Longley, to discuss how their lives had changed since the incident.

Following the fire, Great White split into two separate groups, one led by Russell and the other by Kendall. Neither version of the band performed in any of the six New England states for over a decade. Russell's group made its first New England appearance in 12 years at a harvest festival in Mechanic Falls, Maine in August 2015.

The site of the fire was cleared, and a multitude of crosses were placed as memorials, left by loved ones of the deceased. On May 20, 2003, nondenominational services began to be held at the site of the fire for a number of months. Access remains open to the public, and memorial services are held each February 20.

In June 2003, the Station Fire Memorial Foundation (SFMF) was formed with the purpose of purchasing the property, to build and maintain a memorial. In September 2012, the owner of the land, Ray Villanova, donated the site to the SFMF. By April 2016, $1.65 million of the $2 million fundraising goal had been achieved and construction of the Station Fire Memorial Park had commenced. The memorial dedication ceremony took place on May 21, 2017.

Investigation
In the days after the fire, there were considerable efforts to assign and avoid blame on the part of the band, the nightclub owners, the manufacturers and distributors of the foam material and pyrotechnics, and the concert promoters. Through attorneys, club owners said they did not give permission to the band to use pyrotechnics. Band members claimed they had permission.

A National Institute of Standards and Technology (NIST) investigation of the fire under the authority of the National Construction Safety Team Act, using computer simulations with FDS and a mock-up of the stage area and dance floor, concluded that a fire sprinkler system would have contained the fire long enough to give everyone time to exit safely. However, because of the building's age (built in 1946) and size (4,484 square feet [412 m2] ), many believed the Station to be exempt from sprinkler system requirements. In fact, the building had undergone an occupancy change when it was converted from a restaurant to a nightclub. This change dissolved its exemption from the law, a fact that West Warwick fire inspectors never noticed. On the night in question, the Station was legally required to have a sprinkler system but did not; outcry over the event has sparked calls for a national Fire Sprinkler Incentive Act but those efforts have so far stalled.

On December 9, 2003, brothers Jeffrey A. and Michael A. Derderian, the two owners of The Station nightclub, and Daniel M. Biechele, Great White's road manager at the time of the fire, were each charged with 200 counts of involuntary manslaughter – two per death, because they were indicted under two separate theories of the crime: criminal-negligence manslaughter (resulting from a legal act in which the accused ignores the risks to others and someone is killed) and misdemeanor manslaughter (resulting from a petty crime that causes a death). The brothers pleaded not guilty to the charges, while Biechele pleaded guilty. The Derderians also were fined $1.07 million for failing to carry workers' compensation insurance for their employees, four of whom died in the blaze.

</snip>


February 20, 2019

57 Years Ago Today; John Glenn is first American to Orbit the Earth

https://en.wikipedia.org/wiki/Mercury-Atlas_6



Mercury-Atlas 6

Mercury-Atlas 6 (MA-6) was the third human spaceflight for the U.S. and part of Project Mercury. Conducted by NASA on February 20, 1962, the mission was piloted by astronaut John Glenn, who performed three orbits of the Earth, making him the first U.S. astronaut to orbit the Earth.

The Mercury spacecraft, named Friendship 7, was carried to orbit by an Atlas LV-3B launch vehicle lifting off from Launch Complex 14 at Cape Canaveral, Florida. After four hours and 56 minutes in flight the spacecraft re-entered the Earth's atmosphere, splashed down in the North Atlantic Ocean and was safely taken aboard USS Noa.

The event was named an IEEE Milestone in 2011.



Launch

Glenn entering Friendship 7
Glenn boarded the Friendship 7 spacecraft at 11:03 UTC on February 20, 1962 following an hour-and-a-half delay to replace a faulty component in the Atlas's guidance system. The hatch was bolted in place at 12:10 UTC. Most of the 70 hatch bolts had been secured, when one was discovered to be broken. This caused a 42-minute delay while all the bolts were removed, the defective bolt was replaced and the hatch was re-bolted in place. The count was resumed at 11:25 UTC. The gantry was rolled back at 13:20 UTC. At 13:58 UTC the count was held for 25 minutes while a liquid oxygen propellant valve was repaired.


Launch of Friendship 7
At 14:47 UTC, after two hours and 17 minutes of holds and three hours and 44 minutes after Glenn entered Friendship 7, engineer T. J. O'Malley pressed the button in the blockhouse launching the spacecraft.[ O'Malley said, "the good Lord ride all the way," and then capsule communicator Scott Carpenter uttered the famous phrase "Godspeed, John Glenn." Due to a glitch in Glenn's radio, he did not hear the Carpenter phrase during launch. At liftoff Glenn's pulse rate climbed to 110 beats per minute.

30 seconds after liftoff the General Electric-Burroughs designed guidance system locked onto a radio transponder in the booster to guide the vehicle to orbit. As the Atlas and Friendship 7 passed through max Q Glenn reported, "It's a little bumpy about here." After max Q the flight smoothed out. At two minutes and 14 seconds after launch, the booster engines cut off and dropped away. Then at two minutes and twenty-four seconds, the escape tower was jettisoned, right on schedule.

After the tower was jettisoned, the Atlas and spacecraft pitched over still further, giving Glenn his first view of the horizon. He described the view as "a beautiful sight, looking eastward across the Atlantic". Vibration increased as the last of the fuel supply was used up. Booster performance had been nearly flawless through the entire powered flight. At sustainer engine cut-off it was found that the Atlas had accelerated the capsule to a speed only 7 ft/s (2 m/s) below nominal. At 14:52 UTC, Friendship 7 was in orbit. Glenn received word that the Atlas had boosted the MA-6 into a trajectory that would stay up for at least seven orbits. Meanwhile, computers at the Goddard Space Flight Center in Maryland indicated that the MA-6 orbital parameters appeared good enough for almost 100 orbits.

<snip>

Reentry
During Glenn's orbits, Mercury Control had been monitoring the problem with "Segment 51". The Hawaiian tracking station asked Glenn to toggle the landing bag deploy switch into the automatic position. If a light came on, reentry should take place while retaining the retro pack. Given the earlier questions about the landing bag switch, Glenn realized there must be a possible problem with a loose heat shield. The test was run but no light appeared. Glenn also reported there were no bumping noises during spacecraft maneuvers.

Mercury Control was still undecided on the course of action to take. Some controllers thought the retrorocket pack should be jettisoned after retrofire, while other controllers thought the retro pack should be retained, as added assurance that the heat shield would stay in place. Flight Director Chris Kraft and Mission Director Walter C. Williams decided to keep the retro pack in place during reentry. Walter Schirra, the California communicator at Point Arguello, relayed the instructions to Glenn: the retro pack should be retained until the spacecraft was over the Texas tracking station. After the mission was over, the "Segment 51" warning light problem was later determined to be a faulty sensor switch, meaning that the heat shield and landing bag were in fact secure during reentry.

Glenn was now preparing for reentry. Retaining the retro package meant he would have to retract the periscope manually. He would also have to activate the 0.05-g sequence by pushing the override switch. Friendship 7 neared the California coast. It had been four hours and 33 minutes since launch. The spacecraft was maneuvered into retrofire attitude and the first retrorocket fired. "Roger. Retros are firing. ... Are they ever. It feels like I'm going back toward Hawaii.", Glenn radioed. The second and then the third retros fired at five-second intervals. The spacecraft attitude was steady during retrofire. Six minutes after retrofire; Glenn maneuvered the spacecraft into a 14-degree nose up, pitch attitude for reentry.

Friendship 7 lost altitude in its reentry glide over the continental United States, and headed toward splashdown in the Atlantic. The Texas tracking station told Glenn to retain the retro pack until the accelerometer read 1.5 g (14.7 m/s2). Glenn reported as he crossed Cape Canaveral he had been controlling the spacecraft manually and would use the fly-by–wire mode as a backup. Mercury Control then gave him the 0.05 g (0.49 m/s2) mark, and he pressed the override button. About the same time, Glenn heard noises that sounded like "small things brushing against the capsule". "This is Friendship 7 - a real fireball outside," he radioed Mercury Control. A strap from the retro package broke partially loose and hung over the spacecraft window as it was consumed in the reentry plasma stream. The spacecraft control system was working well but the manual fuel supply was down to 15 percent. The peak of reentry deceleration was still to come. Glenn switched to fly-by-wire and the automatic tank supply. This combination had more available fuel.

The spacecraft now experienced peak reentry heating. Glenn later reported, "I thought the retro pack had jettisoned and saw chunks coming off and flying by the window." He feared the chunks were pieces of his heat shield that might be disintegrating. The chunks were pieces of the retro package breaking up in the reentry fireball.

After passing the peak g region, Friendship 7 began oscillating severely. The astronaut could not control the ship manually. The spacecraft was oscillating past 10 degrees on both sides of the vertical zero-degree point. "I felt like a falling leaf," Glenn later said. He activated the auxiliary damping system, this helped stabilize the large yaw and roll rates. Fuel in the automatic tanks was getting low. Glenn wondered if the spacecraft would retain stability until it was low enough to deploy the drogue parachute.

The automatic fuel supply ran out at 1 minute and 51 seconds, and manual fuel ran out at 51 seconds, before drogue chute deployment. The oscillations resumed. At 35,000 feet (10 km), Glenn decided to deploy the drogue chute manually to regain attitude stability. Just before he reached the switch, the drogue chute opened automatically at 28,000 feet (8.5 km) instead of the programmed 21,000 feet (6.4 km). The spacecraft regained stability and Glenn reported, "everything was in good shape."

At 17,000 feet (5 km) the periscope opened and was available for the astronaut to use. Glenn tried to look out the overhead window instead, but it was coated with so much smoke and film that he could see very little. The spacecraft continued to descend on the drogue chute. The antenna section jettisoned and the main chute deployed and opened to its full diameter. Mercury Control reminded Glenn to manually deploy the landing bag. He toggled the switch and the green light confirmation came on. A "clunk" could be heard as the heat shield and landing bag dropped into place, four feet (1.2 m) below the capsule.

Splashdown

The destroyer Noa hoists the Friendship 7 capsule aboard

The spacecraft splashed down in the North Atlantic at coordinates near 21°20?N 68°40?W, 40 miles (64 km) short of the planned landing zone. Retrofire calculations had not taken into account spacecraft weight loss due to use of onboard consumables. USS Noa, a destroyer code-named "Steelhead", had spotted the spacecraft when it was descending on its parachute. The destroyer was about 6 miles (9.7 km) away when it radioed Glenn that it would reach him shortly. Noa came alongside Friendship 7 seventeen minutes later.

One crewman cleared the spacecraft antenna and another crewman attached a line to hoist Friendship 7 aboard. After being pulled from the water the spacecraft bumped against the side of the destroyer. Once Friendship 7 was on deck, Glenn intended to leave the capsule through the upper hatch, but it was too hot in the spacecraft and Glenn decided to blow the side hatch instead. He told the ship's crew to stand clear and hit the hatch detonator plunger with the back of his hand. The detonator plunger recoiled, and slightly cut the astronaut's knuckles through his glove. With a loud bang, the hatch was off. A smiling Glenn got out of Friendship 7 and stood on the deck of Noa. His first words were, "It was hot in there."

The astronaut and spacecraft came through the mission in good shape.

</snip>


Godspeed, John Glenn!
February 19, 2019

Don Newcombe, one of the greatest pitchers in Dodger history, passes away at age 92

https://www.turnto23.com/news/state/don-newcombe-one-of-the-greatest-pitchers-in-dodger-history-passes-away-at-age-92



Don Newcombe, one of the greatest pitchers in Dodger history, has passed away at the age of 92.

The Dodgers released a statement this morning announcing Newcombe's passing. Newcombe "reached the pinnacle of his career" in 1956 after winning both the Cy Young Award and NL Most Valuable Player awards as a Dodger, the Dodgers tweeted this morning.

Newcombe passed away at the age of 92 after "a lengthy illness."

https://twitter.com/Dodgers/status/1097931542112792576


Cross gently, Don...
February 19, 2019

What if Trump was born to a family without money?

Thought exercise; what do you think his occupation would be?

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